Got up again feeling restless, I walked into the shop to look at the newly assembled mill. I broke one of the handwheels a while ago and have been thinking of getting it fixed. I remembered the warning on all forums not to operate any machines while under medication. I reasoned that I can still do light milling safely.
After fiddling around to remove the stiffness in X-axis, I proceeded to drill out a slightly bigger hole to fit an M5 button head SHCS.
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The hole was progressively enlarged till the M5 screw cam slide in easily.
A flat is milled at the back of the handwheel to allow the screw to be tightened flat.
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Next, some threads were removed in the middle section of the screw so that the plastic sleeve can rotate freely. This took a bit of time as the screw kept wanting to move out of the 3 jaw chuck.
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Two nuts were used in the assembly; one against the face of the handwheel to stop the screw from loosening, the other loctited at the tip of the screw. The plastic sleeve was also shortened a little to fit.
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The handwheel mounted. Works rather well! Glad to be able to save some money for other more useful stuff.
From the experience of using the manual mill, I found it to be easier to feel how fast I need to feed the stock to tool. With more practice, I should be able to determine what feedrate to set for CNC operation.
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